I realize that a new intake might indeed be what is needed to remedy this. Just the nature of the beast, I suppose.
Confirmed that the RTV I smothered in between the two mating surfaces does indeed work. I sprayed it down with some brake cleaner at idle and it didn’t increase/decrease RPMs. Showing some promise there. If this works I will take it apart again and put a thin bead of RTV on both sides of the gasket so it doesn’t look like complete crap.
I did have a lean code that was stored in the ECU but did not produce a CEL. Though I’m not sure if it was before or after the application of RTV. I should have broke out my laptop and pulled the freeze frame data but was lazy and used my cheapo Bluetooth scanner to pull it. I’ve cleared it and will see if it returns during the next few drive cycles.